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AsparagusMike

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Posts posted by AsparagusMike

  1. Had some some fresh rubbers installed over this last weekend. Last set was starting to become a bit of a hazard to drive on.

    IMG_20200418_102250.jpg

    This was one of the better ones of the 4 on the old set.

    I decided to go with the same exact ones I had, Toyo proxies r1r. The overall performance of them were better then expected and for all the abuse I put them through I was surprised they lasted as long as they did. Also, they were my best option being that I only have four tires to pick from on tire rack in a 225/45r16 (who by the way have the best selection in that size)

    After having the new tires installed I had the car re-aligned.

    It really is quite amazing what a fresh set of tires does to the handling of a car! 

    IMG_20200419_195141.jpg

    So on another note. My drivers seat had some adjust-ability and support issues so I pulled it out and started dissecting. It didn't take me long to find out my issue...

    Screenshot_20200427-205849.jpg

    The other side of the bracket was cracked in the same place. Took the seat over to my buddies that afternoon and had him throw a weld on both sides.

    IMG_20200424_162933.jpg

    Yes I understand how jank as hell this is but I have been hardcore shopping for a nice set of used seats that would fit me and what I use the car for best and have so far been unlucky. For now this will work and I hope to find something to replace it within the next month or so.

  2. Differential was fully dissembled for the case and cover to be sent in for sand blasting.

    IMG_20200310_214109.jpg

    That Thursday I dropped the case and cover off at a local industrial painting shop. I stuffed the casing full of newspaper and duct taped the holes to help prevent to much sand from getting inside or hitting the bearing races for the pinion gear shaft.

    IMG_20200311_204425.jpg

    The following day after work I picked them back up.

    IMG_20200313_151735.jpg

    As for the smaller components I threw a wire wheel on a die grinder and went to town cleaning them up. 

    IMG_20200312_192606.jpg

    After going through and de-greasing/blowing everything off I prepped all the metal with some por-15 metal prep to add an extra etch to the metal for better adhesion.

    IMG_20200313_162849.jpg

    It's a pretty simple task, just simply brush it on all the areas where paint will be applied and let it sit for a half hour. Once a half hour has past rinse everything off with water and your set to go.

    IMG_20200313_164006.jpg

    Did two medium coats of por-15 waiting about an hour in between coats. After the last coat I let it dry for a full 24 hours.

    IMG_20200314_123732.jpg

    While the paint dried I started on the lsd rebuild. As a refresher this is getting the 3 clutch disc upgrade from thayer motorsports increasing the lock up to around 50%.

    IMG_20200314_162757.jpg

    The rebuild is very straight forward and Thayer includes a link on their site with a step by step process. Biggest thing here is taking your time and double and triple checking yourself making sure everything is in the right order facing the correct way. After removing all the guts I did soak the lsd unit in de-greaser cleaning it thoroughly before beginning reassembly. Remembering to lubricate every component with diff oil as it is being installed is crucial. Left over parts after the rebuild was the two old clutchs and dog ears, 4 mm spacer that the third clutch takes the place of and the eight old carrier cap screws.

    IMG_20200315_203719.jpg

    The following day I removed the masking off everything and cleaned everything once more through. I also threw a few light coats of satin clear to the diff cover to protect from corrosion.

    IMG_20200315_204920.jpg

    First part of the rebuild is reinstalling the rear pinion gear. I did replace the clamping bushing and the dust cover. After inspecting the bearings I chose to reuse the original ones as they were still in good shape. Being that I hadn't changed anything with gear clearances I simply torqued the nut down to 137 ft lbs as specified from bmw and what I confirmed on a couple threads on other forums and called it good.

    IMG_20200315_215429.jpg

    After installing the freshly rebuilt lsd with the ring side retainers and axle shafts I took a little red paint and brushed it on the ring gear and spun it a full turn to ensure that the gears were still properly meshing. I also checked for any crazy amounts of backlash which was also within spec.

    IMG_20200316_174454.jpg

    Used some permatex "the right stuff" gasket maker to seal the diff cover to the diff.

    IMG_20200316_180040.jpg

    After ensuring the preload of the pinion gear was within spec I popped in a new locking plate for the nut.

    IMG_20200316_200024.jpg

    Added 1.75 qts of castrol 75w-140 diff fluid which includes the lsd additive needed for the clutch plates. Also popped in the speed sensor with a new o-ring and metal plate. She is ready to be installed in the car.

    IMG_20200316_202209.jpg

    3.73 diff that was in the car on the right.

    IMG_20200316_205541.jpg

    On to the next thing. In a previous post @KaiserRolls mentioned the detent pins in the zf trans. I had not looked into these and did a bit of research as well as checking that it didn't need the replacement done. One of the major signs of failure was the shifter not popping back to center after pulling it out of 5th gear. Luckily everything still felt good.

    IMG_20200313_154902.jpg

    New guide tube came in and the damaged one from the clutch disc was replaced.

    IMG_20200313_184504.jpg

    IMG_20200313_190204.jpg

    After that was all said and done and the clutch disc was flipped around the correct way the trans was re-installed.

    Also installed a fresh guibo

    IMG_20200317_205656.jpg\

    For the manual e36's the 325i guibos were thinner and a bit smaller while the e36 m3 guibos were slightly larger and thicker. If you chose to run the m3 guibo which I preferred the dssr has to be modified. They usually are bent in order to add clearance. Being that I would have had to make a whole new dssr I instead chose to grind away the area that came in contact with the guibo. I over did it on the grinding in order to insure I had no clearance issues. I always knew about the bent dssr's but never knew why until now.

    IMG_20200317_214839.jpg

    IMG_20200318_180925.jpg

    After re-installing I found that I had plenty of clearance now.

    IMG_20200320_221118.jpg

    Up next... brake cooling. About a year ago I drew these up on Solidworks in a class I was taking and had them cut out on the water jet. As for the tubing portions I had some left over 2.5 inch stainless exhaust tubing laying around that I cut into sections and had my buddy tig weld them up.

    IMG_20200308_161644.jpg

    In order to get the adapters for the air ducts on the valance attached I picked up some jb weld plastic bonder. The stuff is designed to attach plastic to metal so I thought I'd give it a try. After letting it dry for about an hour it was solid and definitely not coming off. 

    IMG_20200321_135110.jpg

    Towards the beginning of March I ordered some ducting tubing 2.5 inch on amazon. I ordered two 1 meter sticks which would be more then plenty for both sides.

    IMG_20200319_182429.jpg

    Unfortunately, I did not take any pics of the backing plate installed but it fit up really well. I did have to cut out the original dust shield in order to fit these up. My bigger challenge with this hole setup was where to route the ducting. Originally I thought I'd just run it right through the hole that the factory duct ran through but I ran into issues with the wheel rubbing on it when turning in. I found that my only option was to route straight back and then along the bottom of the frame rail up to the front. 

    IMG_20200322_120734.jpg

    I didn't really have any other method to hang it other then zip ties so I got some beefier ones to make sure it was tight in place but not to tight that it would collapse the tubing.

    IMG_20200322_120728.jpg

    IMG_20200322_120723.jpg

    Plenty of clearance with the wheel turned in and enough flexibility with it all the way out.

    IMG_20200322_121355.jpg

    After this was finished I had the car back on the ground and buttoned up the last little bits and pieces. The same day I took the car out for a short drive around the neighborhood and I found the car was running really rich and there was a ton of drone in the cabin. After taking a look through tuner studio I had found that I had left the flex fuel sensor settings enabled and it was messing with the tune. After disabling it the car was back to normal running at the right afr's and no more drone.

    I never did take any pics or mention anything about it but I did get a flex fuel sensor installed. I ordered a gm sensor which seemed to be the popular option among many tuners. I ran the sensor on the feed line right below the intake manifold where it goes from hard line to rubber hose. I ordered a gm pig tail as well and wired that in except for plugging it into the ms unit which I decided on waiting to do tell I get the car back into the tuner to get it tuned for 91 octane fuel so I have the option to run both e85 and 91.

     

    IMG_20200325_183303.jpg

    The following Sunday morning I took the car for a drive down to the local gas station and ran it through the car wash. First impressions with the new setup were pretty great. The zf trans shifts so smooth compared to the g260 and with the power numbers I am making it handles it so well. The stage 3 clutch surprisingly does not feel that much heavier over the stage 2 and with the zf trans the pedal feels like it is much less grabby and has a more consistent feel. Right away I took the car for a 25 mile drive of very easy driving to break in the new lsd clutch packs properly.

    IMG_20200322_094950.jpg

    Still on the list to get done is finding some replacement seats and ordering some fresh rubber for the upcoming season. Very excited for this summer and really hoping this pandemic pans out soon.

     

     

  3. 8 hours ago, jc43089 said:

    Nice progress.  fyi no teflon tape should be used for -an fittings, only on tapered pipe threads.

    I miss wrote on the post. the threads on the 45 degree elbow going into the flange fitting was not a -10 an, just regular threads (not sure on size or pitch though, probably like m14 I think). The plan was to use some blue Teflon which I guess was oil resistant but happy I just welded instead.

    1 hour ago, m42b32 said:

    I ran into the exact same information about the fx racing clutches. Their instructions that come with the clutch are wrong. I installed mine "backwards" and have had zero issues. 

    Glad to hear it. I'd email them about it but I already know how that would go.

    1 hour ago, B C said:

    I love that oil cooler mount 👍🏼

    Thanks!

    1 hour ago, KaiserRolls said:

    Did you replace the detent stuff on the zf when you had it out? Or where they not bad yet 

    Honestly, after I read this post I had to look up what the hell you were talking about. Never even knew this was something that was a common issue for these. Heading over to the shop in a bit here and I will have to check it. Thanks!

  4. So as usual I've been doing a terrible job of making any updates. A lot of progress has been made over the last few weeks so lets get yall caught up.

    Flywheel is back and on as well as the clutch and trans. While I was in there I did of course replace the pilot bearing to except the larger shaft of the zf trans as well as replace the TOB with a fresh one while i was in there.

    IMG_20200221_203911.jpg

    IMG_20200221_212326.jpg

    IMG_20200221_225003.jpg

    and back in the car she goes.

    IMG_20200223_185336.jpg

    Next off I received a fresh heater core. Got the old one pulled and new one installed as well as replacing the o-rings on the tubes to insure no leaks.

    IMG_20200211_193809.jpg

    Old one was rough

    IMG_20200219_203418.jpg

    IMG_20200223_135255.jpg

    Also installed the rest of the coolant system and air lifted the system to insure there were no leaks anywhere else, non were found.

    re-attached the shifter assembly as well as bled the slave cylinder.

    IMG_20200223_185305.jpg

    Got a feel of the new clutch pedal weight and I must say I think it feels quite more consistent through out the travel of the pedal compared to the g260 (or maybe its just me)

    Next up was reattaching the turbo. Before doing so I went ahead and replaced the old leaky line with a fresh oil drain -12an line from improved racing.

    IMG_20200227_191909.jpg

    The adapter that connected to the flange coming off of the drain side of the turbo however was also leaking. the flanged piece was threaded for -10 an line which then had a -10 to -12 conversion 45 degree elbow which attached to the oil line. Where these two pieces threaded together was not a strong joint and actually leaked quite bad so instead of having to try to re Teflon the threads in hope of no more leaks I measured up where that piece had to sit in order to clear the cold housing of the turbo and the manifold and had my buddy weld it together.

    IMG_20200228_212025.jpg

    It fit perfectly however it is a very snug fit.

    IMG_20200228_215212.jpg

    Next up was the front mount intercooler and intake. Before re-installing I wanted to thoroughly clean both out with acetone in order to insure clean flow through the intake system.

    IMG_20200302_212829.jpg

    I let the acetone sit in the intercooler sealing it off on both sides before sloshing it around a bit and then pouring it out. I repeated this about 3 times to insure it was completely free of oil. Same goes for the intake although the intake manifold was much filthier and took a few more times to clean.

    IMG_20200303_165439.jpg

    IMG_20200303_170808.jpg

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    Afterwards I wanted to get a fresh coat of paint on the intercooler. The condition of the paint on it was chipping in many places (as you could tell from the previous pic) and was starting to be a little more visible through the grills. 

    I could tell the first time around the paint had just been sprayed over the intercooler with not much prep or primer. This time the intercooler was roughed up with a scotchbrite pad before applying a couple light coats of etching primer and then a few medium coats of matt black paint.

    IMG_20200303_195146.jpg

    IMG_20200303_204124.jpg

    After letting it dry for 24 hrs it was reattached to the car.

    IMG_20200304_173626.jpg

    Next up on the agenda was replacing the fuel hose above the tank and in the engine bay. These had been replaced way back when the new tank had been installed in the car but unfortunately they were not rated for e85 and I noticed a large amount of cracking on more then half of them. I went ahead and picked up some e85 rated 5/16 fuel hose from a local auto parts store and got to it.

    IMG_20200308_174739.jpg

    While I was in there I installed a fresh fuel filter while it was apart. I did pop the pump assembly off and glance in the tank to make sure things were all good, which they were. Before storing the car for the winter I topped off the tank with e85 and added some stabil 360 ethanol rated. The idea behind that was to help prevent the ethanol from eating at the inside of the tank and hopefully prevent it from absorbing moisture as quick. I thought for shits and giggles I'll test it and see what the ethanol content of the fuel was after sitting for 4-5 months with the stabil in it. Sure enough it was still at 80% ethanol which was awesome.

    IMG_20200309_171829.jpg

    With this checked and complete I got the rest of the motor back together and what not. This brings us to this last Sunday. Everything was done up to the point that I could at least run the motor and make sure it was all good before proceeding on to other things on the list of to-do's. Well, after a motor has been sitting for a while I like to crank it over several times to get oil pumped through before actually starting it. For mine, it's tell I see oil coming out of the turbo feed line which I had disconnected and running into a plastic container. So I start cranking and about 2 or 3 seconds in I hear this terrible, ear piercing screeching. I immediately stopped and tried it once again and sure enough it kept on screeching, sounding like it was coming from the bell housing. I called it a night to think on it. The folllowing day I came back and popped a wrench on the crankshaft bolt and started spinning the motor slowly by hand and as expected it was coming from the bell housing but I still wasn't sure what was causing it all I knew was that the trans had to come back off.

    That same evening I got right to it and after about an 1 hr of fiddling around I had the trans back off and almost immediately saw my issue.

    IMG_20200310_183108.jpg

    The guide tube had been rubbing on the clutch disc which had caused it to mushroom up. This only meant only one thing, I had the clutch installed backwards. That was confusing for me though cause I recalled following exactly as the instructions had said from fx racing which said to have the hub/protrusion face the trans. After digging around on the intranet I found that I wasn't the only one who had run into this issue and people had started the engine causing the tube and disc to build up so much heat between each other that they ended up friction welding themselves together making it quite the challenge to pull the trans back off. It came down to the fact that the instructions were actually incorrect from fx racing and that the hub on the clutch disc has to be facing the flywheel. Frustrated but thankful it wasn't something worse I got the disk flipped around and the pressure plate re-installed. I do want to point out that I installed the clutch disc the same way when I had the stage 2 kit. However for some reason with the g260 the guide tube never meshed with the disc so I guess if you're running the 260 on a 24 valve you shouldn't technically have any issues running the disc that way.

    IMG_20200310_204405.jpg

    I did go ahead and order a new guide tube from the dealership which should be showing up tomorrow sometime and I should be able to get the trans back on the motor this weekend.

    Yesterday and tonight I was able to begin disassembly of the differential and the casing sent off to get sand blasted. It should be done tomorrow and ready to be picked up. The plan is to get that back and repainted, re-built, and installed in the car. We shall see how that goes.

     

  5. Couple parts from my E30 I know longer need.

    Getrag 260 transmission. Solid trans overall. Output and selector rod seals have been replaced. Comes with slave cylinder that has about 10,000 miles on it. Ran redline MT-90 fluid in it and shifts into every gear smoothly. $SOLD

    IMG_20200210_210151.jpg

    IMG_20200210_210201.jpg

    IMG_20200210_210215.jpg

     

    M20 reman'd driveshaft. Was purchased from Driveshaft Specialists out of Texas last Spring. Has roughly around 5,000 miles on it. Everything still feels tight (U joints, center support, etc.). Comes with Fairly new guibo. Purchased it for $400, looking to get $SOLD

    IMG_20200209_205412.jpg

     

    Condor E30 24 valve G260 trans swap brace. $40 obo

    IMG_20200209_205323.jpg

    IMG_20200209_205312.jpg

     

    E30 Control arm brackets with 90a center revshift poly bushings. $SOLD

    IMG_20200209_203017.jpg

     

    Let me know what you need!

  6. 8 hours ago, B C said:


    I went with bronze because the last trans I refreshed had a black plastic one worn into the shape of a new tube of lipstick (what!?).

    I dont disagree that plastic works, im sure they last 30k miles just fine and that is a lot of summers worth of miles

    Ya and if it doesn't last that long then I guess I'll have to pull the trans again. At this point with how many times I have pulled the motor it ain't no big deal to me. 😀

    10 hours ago, jc43089 said:

    Is that blue flywheel a UUC Motorworks one?  If it still in decent condition I might be interested.  I've got one in the drivetrain that is in the van but I'd like another one in my DD coupe.  The heavy stock flywheel is terrible after having experienced a lightweight one.  Why are you switching to Chromoly?  Nice progress on everything.

    It is not. It's the fx racing's lightweight aluminum flywheel which was an amazing flywheel for the money and I really liked it. The reason for switching is because I am unable to to purchase a replacement friction surface plate. I wanna say right of the bat that gripforce.com has TERRIBLE CUSTOMER SERVICE! I have tried multiple different times to try to call them and every time it goes to voicemail. The only way to get a hold of them is through email which is fine, if they'd answer them in a timely fashion! The first time it took me 3 times to email them before responding by telling me they have not yet come out with a replacement friction plate for their aluminum flywheels but they can offer me a discount on another one of their aluminum flywheels. I was fine with that and then had to email them 7 MORE TIMES asking them what the final price would be after the discount for them to respond that their aluminum flywheels were on back order and they could not help me. Terrific! Luckily I had a fx racing chromoly flywheel sitting around from another car, slightly used, that I decided to get resurfaced and use instead. The chromoly is only about 4 lbs heavier over the aluminum one and from what i've seen from other 24 valve e30's running them, they seem to perform just as well.

    I will however be using the aluminum flywheel and stage 2 clutch and pressure plate for another car so I'm not looking to get rid of them.

  7. 1 hour ago, B C said:

    Have you seen the bronze clutch fork pivot pins?

    I have and honestly I don't think they're that much better or worth the extra money. Before I installed the g260 on the motor way back when, I had replaced and installed a fresh oem pivot pin. When I pulled the trans off this last weekend (10,000 miles or so later) the pin barely showed signs of any wear. After seeing this I thought I'd just stick with the oem one. I have also went out and read other threads of people having issues where the brass ones were not lasting all that long and prematurely wearing because of the brass being to soft. 

  8. Last season was a blast! Car felt near bulletproof throughout the summer but there were a few issues that need tending to.

    The transmission. G260 + Boost = Ticking time bomb. Also the gearing could be a little longer, So I'm switching it out for the zf trans.

    Picked up a zf trans from a local junkyard. Overall condition is not to bad. Trans was pulled from an e39 528i.

    IMG_20200110_115657.jpg

    Also snatched up a 2.93 lsd diff to sit behind the zf. Hoping it should make for decent gearing for the power level I'm at. Plan is to rebuild it. It will be getting a 3 clutch disc upgrade to hopefully reach a little more lock up. (40 - 50% I believe)

    IMG_20200106_151711.jpgi d

     Unfortunately ever since this car ran with the turbo the oil drain line fittings leaked from the back side caking oil all over parts of the engine, skid plate and car. Should have replaced it sooner buuuuutttt I was lazy so i put it off and now I get to deal with it now.

    IMG_20200208_202717.jpg

    Luckily we hit a patch of warm weather for one day and I ripped out the pressure washer, de-greaser and a scotch brite pad and went to town on all the oil and grease on the transmission casing.

    IMG_20200202_144731.jpg

    After a good cleaning I got right down to it and replaced a few things.

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    Seal replacement went really well with no major issues along the way and is now all ready to be installed besides the throw out bearing which I had forgotten to order but is now on its way.

    As I started disconnecting the driveshaft and shifter linkages I noticed some blue coolant dripping from the drain ports from the heater core box, great. I had noticed that my coolant level had dropped a good amount over the season but I made sure it never completely emptied itself. Nevertheless I have added to the list to replace the heater core.

    IMG_20200208_194230.jpg

    After a few more disconnections...

    IMG_20200209_165416.jpg

    A while back I noticed quite a bit of shaft play on the turbo and thought it might be nice to go ahead and rebuild it.

    IMG_20200208_210807.jpg

    I must say It is quite nice having a turbo with a very reasonably priced rebuild kit. I am also quite impressed with everything that it comes with as well. Kit was from turbo labs of America.

    IMG_20200215_122554.jpg

    Rebuild process went very well. I was a little nervous at first but quickly realized how easy rebuilding one of these actually is, as long as you take your time. Only challenging part was the removal of the smaller snap rings that hold in the small thrust bearings but otherwise everything else came apart and went together no problem.

    IMG_20200216_172720.jpg

    After pulling the g260 off the motor and clutch/flywheel. clutch disc still looks pretty good with no unusual wear. Even though it worked out well most of the time there was a few times during hard pulls from 3rd to 4th gear I could feel it slipping and truly it was at its max if not over what the max for what it was rated for. Luckily when I picked up all the turbo goodies way back when, there was a brand new stage 3 clutch and pressure plate thrown in with everything else as part of the deal so I will be using that as well as switching over to a chromoly flywheel that I am getting resurfaced by a local machine shop this week.

    IMG_20200210_200008.jpg

    Now that the DSSR was all nicely welded up at 10 degrees it was time to turn it back. There was a few options to do this but I found it easiest to just heat it up red hot and twist it. Called up my buddy who had an oxy acetylene torch and he made that happen. we did figure out that even at red hot we were gonna need better leverage then a screw driver through the holes. A pipe wrench was used instead which worked terrific!

    IMG_20200215_190104.jpg

    Did my best to polish it up afterwards with a scotch brite pad.

    IMG_20200216_172733.jpg

    Lastly I picked up some solid control arm mounts from condor back during their black Friday sale. I wanted to try and get a bit more caster for the front wheels and I have heard really good things about these in terms of handling. Install was easier then changing a battery.

    IMG_20200209_202926.jpg

     

    And that's what I have done so far. Ordered quite a few parts last Friday night that should hopefully be arriving sometime later this week. If all goes well I should be able to get the engine back in the car this weekend. Besides getting the diff rebuilt that will be it for drvietrain stuff, at the moment.

    There are Couple other things on the check off list.

    1. I plan on installing a flex fuel sensor. Come spring time I hope to get the car tuned to run on 91 octane. For the most part I do plan to continue running the car on E85 cause mo power! Its more for when I find myself in an area where E85 is less prevalent.

    2. Make some holes where the eccentric hardware are located. With the subframe raised in the rear to fix excessive negative camber there is no longer any room to fit wrenches to adjust them. More to add to this later.

    3. Front brake duct cooling kit

    4. Different pads and rotors set up

    5. Different seats. Still looking around at what I'd like to get, all I know is the seats I have currently have to go. I originally wanted to rebuild/re-upholster the seats but at this point I would rather run something different completely. Still hunting around though.

    Maintenance to-do's before returning to the streets...

    1. Oil change

    2. Clean intercooler

    3. Flush brake fluid

    4. Swap out spark plugs

    5. Replace air filter

    6. Drain fuel

     

     

     

     

     

  9. On 1/23/2020 at 6:51 PM, GunMetalGrey said:

    I brought this car up today to Brian, and it made me wonder if anything has happened to it as of late.
    Or are you just working on farming the 'sparagus?

    As of right now the car has been sitting in storage collecting dust. Have a few big things in the works for it to get done before spring time roles around. I've been accumulating parts over the last few months and hoping to get er in the shop within the next 2 weeks. Updates coming soon! 

  10. 19 hours ago, YoungCR said:

    @AsparagusMike had his car tuned recently.

    Hunter Mulhollon

    He has a dyno in his shop. Very good with MS tuning and TS and his prices are pretty reasonable. 10/10 recommend

    Located on the north side of Fond du lac.

    He did some re-tuning on my car (running MS3 pro) a little over a month back and it has been running flawless ever sense.

    Shoot him a message on Facebook, super nice guy and he knows his shit.

  11. Update:

    Brakes came in Friday!

    20190621_170402.jpg

    After work I buckled down and spent a few hours tackling all 4 wheels.

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    20190621_185108.jpg

    Once the brakes were done and the car was back on the ground I took it for a little drive to get the pads properly burnished in, all ready to go for Sunday.

    Well Sunday morning came and I had a bit of a late start from the night before. It was roughly 7:30 when I woke up and I was two hours away from the track. The two hours was not including the fact that I still had to get home to grab the car plus pick up two people, stop for fuel and make it there before ten. Well needless to say I made it to the track... at 10:20. I get inside to find out that my spot had been taken and I wasn't gonna be able to run. I was pretty bummed out at that point as I had been looking forward to driving this track for some time now. I decided to stick around anyways as once they started sending cars out I was able to hop in and ride with another fellow e30 driver who was also quite fast (turbo M20) and I learned quite a bit as well as had a blast. After they got midway through heat four I noticed a car at the starting line who had its hood popped open smoke going everywhere with coolant spilling all over the track, it was the same guy who had replaced me and his car had overheated. I wanna give a huge shout out to @KaiserRolls who approached Tom (the main man running the event) a few minutes later and asked him if I could drive in place of the guy with the crowd killer (found out later his name was Jake) if he would be willing to give up his spot so I could drive the last four laps of round two. Tom acknowledged the idea and so I approached Jake and after chatting with him for a few minutes and informing him that this was my first time doing auto-x he happily gave his spot to me for the last portion of the event! I was in! 

    Once we got the numbers swapped over on to my car and tech inspection was passed I was in line ready to go for the fourth heat which was being combined into four laps one after another (hot lapping) in order to get everyone through more quickly and avoid the rain which was beginning to approach us. As a way of expressing my appreciation I offered to let Jake ride along with me on my first lap which he gladly accepted.

    I never quite realized how crazy 400 hp in a light car such as the e30 was until I took it out on a proper track like US air raceway. It is quite a lot to handle and makes things really interesting when it comes time to stop to make a turn. I knew going out I wasn't gonna be setting any crazy times and more just wanted to enjoy the car on this incredibly fun track and get a feel for it. Unfortunately I didn't notice to much of an improvement with the hawk hps pads other then the fact that my wheels weren't smoking quite as much by the end of my fourth lap. During my second lap I found out just how little stopping power I had after I was unable to make the last turn to the finish line from the amount of speed I had built and continued straight into one of the a bails of hay which was being used as a wall around the corner. Luckily the car endured no damage other then the valance being slightly pushed in which I pulled back out with ease. For now though I will continue to run with the brake setup I have and just work on not going quite as fast, focusing more on the handling and technique of it.

    Overall had an awesome time, car ran great and I am really looking forward to the events to come.

     

    Now that the car is running properly there is only more thing to do...

    (Potato phone quality video for your pleasure)

     

     

     

  12. Update!

    So last night I took the car over to a man by the name of Hunter Mulhollon (hunter tuned) who knows MS really well and messed around with my tune a bit to figure out why I was cutting out. Luckily he was able to get the car on the dyno the same night and got her dialed in really well.

    First of all, before he did any tuning he went ahead and pulled a spark plug and checked the gap, it was .025. After informing him that I was running a 2 step colder plug and had gaped them all to .021 he pulled the other 5 and found that all of them were in the .025 to .027 range. It seems I was suffering from a bit of spark blowout. He brought them all down to .019 - .020 and popped em back in. After a few pulls he found that I was getting some pretty lean spots on the fuel table. Went through and cleaned that up making everything a bit more fat (rich) for safety and being that I'm running e85. After making some more adjustments else where he did one final pull and the car put down a whopping 400 hp! The crazy thing is the tune is still pretty conservative as I'm only at about 8 lbs (once in a while creeping to 10ish lbs) and running e85. There was actually room for even a little more power safely but unfortunately being that I only have the stage 2 clutch in there now she's about maxed out and he started to smell it slipping a little so he called her quits. The big thing is my cut out issue is now gone and she feels even more responsive! Driving it home I tried about every situation I could think of that would make the car cut out before and she just kept pulling. All in all amazing work from Hunter.

    FB_IMG_1561051835055.jpg

    I also just wanna say that Shane at DB performance still did an awesome job on the car and I was very pleased with his work. I think that if my e85 ethanol content had been a little higher with the fuel that was in my tank some of my fuel map values may not have been as lean as they were and I may never had encountered any cut out issues. Overall, awesome job tuning from both Shane and hunter, this thing is a fuckin blast!

    Pads and rotors should be here tomorrow!

    Stay tuned!

  13. Very long and over due update...

    The last 2 months or so have been unbelievably fun with this car and its been exciting to see how competitive she can be against other considerably quick cars.

    Over the month of May I took the car to a couple shows, local meets, and the occasional trips to Mexico. The car has been really good and for the most part has been running spectacular except for the occasional mishaps.

    First off, guibo...

    After about 2 weeks of driving the car I started noticing a lot of vibrations in 2nd and 3rd gear and knew something was up. At first it seemed like suspension so I did a shake down test and while doing this I came upon this.

    20190514_105054.jpg

    When I got the new reman'd driveshaft the guibo seemed alright but with the extra torque it didn't last long.

    Not only did my guibo shred up quite badly but my reverse light wire wasn't tied up enough causing it to droop down resulting in it getting caught in the driveshaft and being ripped out leaving only some wire running to the connector by the shifter. Ended up having to make a new one which I wrapped up nicely above the trans where it should hopefully no longer have any interference with any more moving parts.

    20190516_180634.jpg

    Ordered a new oem guibo through fcp and haven't had an issue sense.

    20190516_150741.jpg

    Next little fun incident I had was my fuel pump assembly o-ring going bad causing fuel to leak out of the top every time I topped off the gas tank.

    20190420_204638.jpg

    It would pool out a good quarter to a half a tank of gas from the top of the tank. After pulling the back seat and access panel I found this knowing right away that's what it was.

    20190420_204649.jpg

    Ordered a new oem ring through the dealer which came the following day, easy swap out. I'm assuming the e85 just took the best.

    20190527_182716.jpg

    Haven't had a leak sense!

    Next up I installed a catch can. The catch can was a much needed item as I had the ccv hose just running down underneath by the skid plate causing a oily mess in the skid plate and the surrounding areas.

    20190422_185041.jpg

    The catch can was a fairly cheap one from amazon but being that I didin't have it recirculating back into the intake I didn't need anything fancy with a good filtration system, just something to catch everything coming out of the crank case. Mounted it in the only place I could find that would make for easy access and fairly clean look.

    20190424_181029.jpg

    No more oily messes!

    This was after a weekend of driving and racing around quite a bit.

    20190512_095933.jpg

    Next up was my fenders. For the most part, my wheel and tire setup have been great but my front tires clearance from the inner fender was tight and was causing quite a bit of a rubbing. Thanks to @GunMetalGrey hooking me up with a fender roller and some guidance I spent a few hours making some better clearances.

    20190428_154432.jpg

    Sense I had all the wheels off and the roller I decided to do the rear as well which oddly enough had been rolled but only halfway on both sides. After checking on a couple other e30's we determined that it definitely wasn't something done from the factory. Nevertheless it made for an easy job on the rears and they went quickly.

    No more rubbing issues!

    Next up was the steering wheel. I had just about enough with the airbag steering wheel and decided it was time for it to go. After spending a week researching and deciding on what to replace it with I decided on a momo steering wheel, the montecarlo.

    20190506_165933.jpg

    20190507_084936.jpg

    Its incredible how much of a difference a slightly smaller better feeling steering wheel can make. The new steering wheel matched with the z3 steering rack makes for an unbelievable feeling that reminds me of driving a go cart, I love it!

    Oh and I also have a horn now lol. The original airbag steering wheel was messed up causing the horn to go off every time I turned it forcing me to pull the fuse and run without.

    Next up, brakes.

    After refreshing the entire brake system I installed centric oem high carbon rotors and stoptech sport pads. This setup worked great with the NA s52 setup and I felt like I had sufficient stopping power. Now with the extra power they are starting to show their weakness. I went out with a couple of friends this last weekend and drove some country back roads with quite a few curves pretty intensely. By the end of it my front wheels were smoking really badly and I even noticed quite a bit of fade on the brake rotor. After seeing this I knew it was time for me to upgrade to something a bit better. I stuck with an oem high carbon rotor but switched over to some hawk hps pads for both front and rear. I was considering doing another step up to the hp+ pads but found that many said they weren't the most ideal if the car is being drivin on the street as they squeak quite a bit. I will see how the hps pads perform and go from there.

    Lastly and most importantly, my cut out issue.

    This is something I've had ever sense I got the car back from the dyno. It happened very rarely at the beginning but as I drove the car I figured out where and why it was happening but wasn't quite sure how i should adjust it.

    Scenario: I'm driving in 3rd gear at about 2600 rpms. If I gave the car 100% throttle right away the car would almost immediately cut out and I would lose all power. I would then let off the throttle completely and let the car roll for a few seconds in which it would then return to normal and I could go along my way with no problem. Now, if I rolled into the throttle in 3rd gear instead of 100% she never cut out and would pull well with no issue. It would also never cause an issue when starting from a dig and revving out all the gears. I started digging through TS a bit and I came upon the afr safety settings. After reading through the settings and thresholds set compared with when the issue was happening I feel that this is what is causing it. After 2500 rpm's when the afr was found to be off by 1.3 lean or 1.3 rich it would kill spark and then fuel tell I let off the throttle for 3 seconds in which it would return to normal. 

    afr safety setting pic.PNG

    Luckily I just recently found a local guy who tunes a lot of standalone systems and is quite familiar with MS and tunerstudio. I'm bringing the car over to him Wednesday and hopefully we will be able to clear up this issue before the weekend.

    Well that's about it in terms of things that were fixed and what needs improvement. For those of you who I didn't get to talk to at the picnic I finally got to take the car to my local drag strip and got to see what she runs in the 1/4 mile. Being that it was my first time doing this I was quite nervous causing my first two runs to a little weak.

    All in all I was able to get in four runs total with my best time on my third run, 12.23 seconds at 118 mph.

    The match was against a Mitsubishi ralliart which had quite a bit of work done to it including a larger turbo and running e85. (Owner predicted it at around 425 hp awd)

    Well, it wasn't quite enough...

    What hurt me the most was my 60 foot which was about 2 seconds. I think I should be able to shave off a good .3 seconds off of that but it's a bit challenging being that trying to launch the car at all results in me spinning a little tire.

    I had a lot of fun overall and it was a great experience.

    Snapchat-1149581879.jpg

    As for upcoming events I am excited to say that I will be participating in my first auto x event this Sunday at the US air motorsports raceway in Shawano. Hoping to see a few of you guys there!

     

    Burnout vids coming soon.

    FB_IMG_1560119037509.jpg

     

     

     

  14. I had an awesome time walking around checking out all the different setups people were running and chatting with them about it. I must say I was a bit surprised at the amount of 24 valve swapped cars that were there.

    On the down side I made the mistake of forgetting sun screen and my arms as well as the back of my neck were bright red by the time I got home.

    I do hope we can get a couple cruises going this summer, I really enjoyed hanging out with everyone!

  15. As long as the route has a gas stations with e85 along the way I would be totally down for a cruise! 

    If your planning something in June I would only be able to make it if its either on the weekend of the 8th (which is the picnic anyways) or the weekend of the 22nd. I work on the opposite weekends unfortunately.

  16. 23 hours ago, GunMetalGrey said:

    Also, I think I know where your oil is going. Watched the dyno pull vid and saw the let off cloud 

    Ya No doubt my car is consuming a bit of oil. I have been monitoring it frequently though and it doesn't seem to be much worse then it was when the motor was NA.

    About a quart every 1000 miles... 1/4 of a quart give or take every 2 tanks of gas or 300 miles.😁

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